REAR-END COLLISION OF
UNION PACIFIC RAILROAD FREIGHT TRAINS
EXTRA 3119 WEST AND EXTRA 8044 WEST NEAR KELSO, CA.
On Monday, November 17, 1980 a disastrous
rear end collision occurred five miles west of Kelso, caused by a runaway
train descending the hill. Three crewmen were killed and a fourth
critically injured. Early in
the afternoon Extra 3119 West, a U.P. work train carrying 20 cars of ties
from Las Vegas to Yermo was stopped in the siding at the top of the
hill at Cima. The 3119 did
not have working dynamics and the crew was setting retainers, as required
by the rules, for the trip down the grade.
The speed limit down the grade for this train was 15mph. The Engineer of Extra 3119 West was never
again able to reduce the speed of his train. At 2:13pm it was accelerating
at the rate of 1.6mph per minute, traveling 19.5mph. The Conductor pulled
the emergency valve in the caboose but it did little good (the emergency
application never propagated to the front of the train since the
engineer's brake valve remained in service position).
By 2:15pm Extra 3119 was traveling at 25mph and still accelerating
at 5mph per minute and was five miles behind the VAN train. The Engineer on the VAN train ahead,
Extra 8044, realizing what was happening, radioed the Dispatcher asking for
permission to exceed the 25 mph limit for his train. He quickly released
his brakes and opened the throttle, hoping to outrun the 3119 careening
down the hill. The VAN train sped by Kelso at 75mph with the 3119 about a
mile behind, going 62mph and gaining fast.
At 2:24pm the 3119 was by mp241 moving at 80mph, the limit of the
engine’s speed indicator. The 3119 then struck, one at a time, three
of the rear autorack cars, each time derailing and overturning one. The
last hit caused the autorack car to climb up over the 3119, destroying the
carbody and cab of the engine. The
31 year old Engineer and the 21 year old head-end Brakeman were killed
instantly. The railroad was shut down for over 24
hours, until a shoo-fly track could be constructed around the scene.
Amtrak's Desert Wind terminated at Barstow and Las Vegas
respectively. Passengers were bused between
those two stations. The resulting NTSB investigation and report
was highly critical of U.P. and it's rules for brake inspections,
estimating gross tonnage and lack of maintenance of the brakes on the tie
cars. Findings included,
among other things, that the terminal air test performed in Las Vegas was
inadequate and improper. The actual trailing tonnage of the train was over
500 tons more than what the crew was told. Most of the twenty old tie cars that made up the train had
“ineffective brakes” or only “partially effective” brakes. A similar "test" train was assembled and
successfully run down the grade without dynamics, but only after spending
almost two days repairing the brakes on the ties cars! The deceased Engineer, David Totten, was
absolved of any blame for the runaway. |